Two cases of beneficiation plant control
To
conclude the discussion on mineral processing plant control, two case studies
are presented. One is taken from crushing and the other from grinding.
Crushing
Case Study
In the
new millennium crusher control applications in mineral processing will be
largely restricted to primary and autogenous/semiautogenous pebble crusher
applications. Nevertheless, there are still some crushing plants in operation,
and from a pedagogical perspective, some interesting lessons can be learned
from the control work that was performed in these types of operations.
Figure1
provides the process and instrumentation layout required for the example. Because
the secondary crushing circuit was proving to be a bottleneck for overall plant
production, the general objective was to increase throughput.
Fig1. Secondary crusher control process
and instrumentation layout
A number
of control problems in this circuit rendered more traditional methods
ineffective, including the following:
1. Given the scale of the equipment, there was a significant dead time
between the weigh scale
and the
feeders, and between the weigh scale and the crusher.
2. Stockpile segregation meant varying particle size distributions from each
feeder; i.e., the tonnage corresponding
to maximum throughput or maximum power varied depending on the
feeder
configuration in use.
3.Vibrating feeders were prone to both hang-ups and sloughs of material onto
the belt conveyor.
To tackle
these problems, the control engineers began by employing a regulatory loop to
control solids mass flow by manipulating the vibration frequency of the
feeders. Because PID was ineffective, a dead-time compensation scheme was employed to improve the control performance. In addition, and
because the number and specific configuration of the feeders could be changed,
the regulatory control algorithm also included scheduling for process gain
(i.e., based on the number of feeders running) and the estimated dead time
(i.e., based on the specific configuration of feeders running). This proved to
be a very effective approach to achieve good regulatory behavior, and it is of
some interest to see that similar techniques are now used on large
semiautogenous mill feed systems, which suffer the same control problems.
Having
solved the regulatory problem, the supervisory strategy was to ensure maximum throughput.
Because this crusher treated a scalped primary crusher discharge (-200 mm × 19
mm), level control in the cavity is not generally a suitable means of control,
because coarse hard feed will lead to a plugged crusher. (However, level is
monitored to prevent spillage and to aid in control when the ore is fine, soft,
or both.) In this particular instance, maximum throughput generally relates to maximum
power draw.
Given the
variability in size and ore hardness, it is intuitive that the relationship
between power and tonnage is nonlinear. Approaches ranging from fuzzy expert
control to self-tuning controllers have been applied to this nonlinear problem,
but the control engineers in this instance elected to use a clever implementation
of Model-Reference Adaptive Control (MRAC).
To
complete the MRAC installation, the engineers chose to remove tonnage from the
regulatory loop and substitute power. In other words, tonnage was used only for
power prediction purposes, and the dead-time compensation controller was
effectively regulating power.
Previously,
it was indicated that vibrating feeders are prone to sloughing. A large pile of
rock on the belt would cause the controller to make a quick reduction in feeder
speed, but it would soon return to near normal, once the pile passes the weigh
scale. However, this large pile of rock may well be sufficient to plug the
crusher. The operator, who would be responsible for cleanup, would soon switch
the power controller into manual mode, citing excessive downtime, for example.
To circumvent this eventuality, a watchdog function monitors the weight profile
on the belt, and when a large pile is discovered, it will suspend the supervisory
controls, slow the feeders, decrease the belt speed, and hold this condition
until the pile of material is known to have passed through the crusher,
whereupon normal control is restarted. There are numerous other examples of
watchdog control in this specific case, and their existence is one of the
principal drivers behind the embrace of fuzzy expert systems as the platform of
choice for supervisory level automation in mineral processing.
Grinding
Case Study
With
their relatively high capital and operating cost, grinding circuits have been
the focus of much of the attention in industrial process control for the past
four decades. There are other contributing factors, such as the fact that these
circuits are fairly well understood from a phenomenological point of view, and
that in many plants grinding turns out to be the bottleneck in economic
optimization. This latter point often leads to maximum-throughput strategies,
which have the additional complication of accommodating the physical capacity
constraints of the equipment.
Figure 2
is a simplified iron ore processing or
ore lead-zinc mining representation
of the flowsheet for the case study. The control objective is to maximize
throughput while maintaining a product particle size dictated by downstream
production processes.
Fig2.
Flowsheet for autogenous and pebble mill circuit
This
particular circuit was well instrumented and had very good regulatory controls
and welltrained operators using modern control hardware with an excellent HMI.
Nevertheless, frequent changes in ore hardness tended to lead to conservative
operation to avoid overloads. More specifically, in soft ore that is lean in
coarse-grinding media, the autogenous mill operates with low power draw and a
high circulating load of pebbles. The manual supervisory strategy was to set
the fresh feed rate and to change it only when the pebble recycle stream
reached high or low values. In cases where the ore was hard, the autogenous
mill tended to run at high loads and high power draws, with low pebble recycle.
Once again, the manual supervisory strategy was to run at a conservative feed
rate to avoid overloading the autogenous mill (i.e., high charge levels). In
both cases, it was difficult to maintain product particle size, and
opportunities to increase the feed rate were often missed.
In this
case a Model-Based Expert Control (MBEC) supervisory strategy was implemented.
The basic structure for such an algorithm is shown in Figure3. It consists of
the heuristics encoded in the expertise modules, as well as deep process
knowledge, encoded in the phenomenological mathematical models.
This
structure utilizes the models to estimate the state of the process, including
the prediction of many variables that would otherwise not be measurable (i.e.,
a soft sensor). Because there are temporal changes in the feed and equipment
characteristics, the model is adapted to ensure a minimum of plant-model
mismatch. Both of these functions are accomplished by embedding the model in an
extended Kalman Filter. One of the outputs of this modeling module is the
current process state, which can be used directly by the expertise modules. The
other is a welltuned dynamic model, which can be used with the process state
information in the optimization modeling module. In this case, the optimizer
simply integrates the model to predict the steady-state results if no
disturbances were to enter the system, under any particular combination of
regulatory loop set points. The results of these steady-state predictions can
then be used to recommend regulatory loop set points that will achieve optimal
grinding performance.
Fig3. Software structure of the MBEC system
Because
the grinding circuit cannot be perfectly modeled, and because there is a need
for watchdog functionality, the expert modules play an important role in the
supervisory control strategy. A particularly important aspect is to filter the
set points coming from the optimizer, because these are based exclusively on
model calculations, which in turn can be sensitive to sensor problems in the
field signals.
Extensive
on-off testing of the MBEC supervisory strategy against the manual model of
operation demonstrated a 6% improvement in grinding circuit throughput and a
much lower variance on product particle size distribution. The economic impact
was not disclosed, although the payback period was said to be a few months.
To
conclude, it is worth noting that the approach taken in this latter case study
is rapidly becoming the industry standard. The use of process models is highly
recommended, and despite any intuitive belief to the contrary. For supervisory
control in beneficiation plant, best
practices mean a mix of expert systems and mathematical models. The exclusive
use of one or the other will likely lead to suboptimal results.
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